Accident Eurocopter AS 350BA N141MK,
ASN logo
ASN Wikibase Occurrence # 56876
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Monday 5 January 2009
Time:10:45
Type:Silhouette image of generic AS50 model; specific model in this crash may look slightly different    
Eurocopter AS 350BA
Owner/operator:Makani Kai Helicopters
Registration: N141MK
MSN: 2424
Year of manufacture:1990
Total airframe hrs:14290 hours
Engine model:Honeywell LTS101-600A-3
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Wiliwili Nui Ridge, Oahu, HI -   United States of America
Phase: Landing
Nature:Passenger
Departure airport:Honolulu-Daniel K. Inouye International Airport, HI (HNL/PHNL)
Destination airport:Honolulu, HI
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The purpose of the flight was to transport a worker to an antenna located on a ridge top at an elevation of about 2,400 feet. The pilot reported that the flight to the location was uneventful and that he completed his prelanding checklist and noted nothing abnormal. Just prior to landing, there was a loss of engine power. According to the pilot, “the engine felt and sounded like it was winding down and rotor RPM was starting to bleed off.” At this point the helicopter was less than 10 feet from the landing site and was not holding altitude. The pilot maneuvered the helicopter so that it touched down and rolled over onto its right side, which prevented the helicopter from falling down the steep slope of the ridge. After the helicopter came to rest, the pilot shut down the engine. Examination of the helicopter revealed no discrepancies with the fuel system. Engine continuity was established. A pneumatic leak check was performed and leaks were identified at the temperature compensator and at the PX acceleration bellows. A test cell run of the engine was completed without tightening any of the pneumatic fittings. During the test cell run, the engine achieved maximum continuous, takeoff, and thermodynamic shaft horsepower. The engine did not surge during transient deceleration and acceleration runs, and was responsive to commanded throttle inputs. No preexisting condition was identified on the engine that would have interfered with normal operation or explain the reported loss of engine power.
Probable Cause: The partial loss of engine power during landing for an undetermined reason.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR09FA072
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB
FAA register: 2. http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?omni=Home-N-Number&nNumberTxt=141MK

History of this aircraft

Other occurrences involving this aircraft
7 July 2002 N141MK Schuman Aviation Company Ltd 0 near Honolulu, Oahu, HI sub

Location

Images:


(c) NTSB

Revision history:

Date/timeContributorUpdates
06-Jan-2009 10:07 harro Updated
23-Jun-2009 11:53 harro Updated
21-Jul-2014 01:11 Dr. John Smith Updated [Time, Location, Nature, Departure airport, Source, Narrative]
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
01-Dec-2017 11:39 ASN Update Bot Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative]
15-Jun-2023 04:23 Ron Averes Updated [[Other fatalities, Departure airport, Destination airport, Source, Narrative]]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org